Drilled out slam panel welds.
Monday, May 18, 2020
Cutting offthe nose
Saturday, May 16, 2020
Front end damage
Time to begin with the front sheet metal.
All of the sheet metal ahead of the radiator has some degree of badly repaired collision damage. Things were just bent back into place enough to give the car back its external appearance.So the lower radiator duct panel, the duct panel support, the bonnet latch upright support, and the bonnet slam panel will be replaced with new sheet metal parts. The inner wings will get some hammer and dolly work.
Fortunately that was the full extent of the rust. The forward outer sill and the inner wing structural areas are all sound. As bad as my luck has been for hidden collision damage, I've gotten lucky with very little rust to offset that.
Thursday, May 14, 2020
FR Wing lower panel replacement
Right side lower wing panel replaced with the new BMH part. Fit was generally very good. I'm glad I changed this out.
The paint on the door was so thick that I had to strip it before I could be sure of the panel alignment. In doing so I discovered that the door is not original. It appears to possibly be a Heritage replacement because of the black epoxy coat I found underneath. But there were at least three paint jobs done on it since it was installed. Yay, a body body panel that didn't need repair!
Friday, May 8, 2020
More new sheet metal
This arrived today from Moss UK. Took about 1 week after order.
With new wing lowers costing only £58.92, I decided to get both sides. All Heritage parts except the radiator duct panel which is Steelcraft (Heritage panel not available.) Total for all the parts here was £373.84 plus £88.00 for Fedex shipping to North Carolina. Still way less than buying stateside. No duty is charged as they are classified as parts for antique cars, below the duty threshold amount, and Fedex doesn't charge import brokerage fees like carriers used by some other vendors (e.g. UPS, and DHL).
Beating out original FR wing
So I decided to have a go at repairing the original fender. As I had feared, stripping the paint and thick bondo revealed crude repair of collision damage. Most of the damage was at the nose of the fender, but there was a substantial bulge in the lower rear panel just aft of the wheel arch.
Forgot to mention, the inner structure was remarkably free of rust, with the original primer mostly intact.
After a few hours of hammer work I got the nose section approximately back to where it belonged. Some cracks and holes from the old body repairs would then need welding.
The radio antenna hole was bent up in the area, and while straightening it, I just decided to close it off completely.
After many hours (days) of hammer and dolly, heat shrinking, and welding, I got most of the bulge worked out of the lower panel and the wheel arch mostly corrected.
Got some Dyna-Glass filler on the fender. But still not satisfied with the lower panel. It still curves outward a tiny bit more than it should. No amount of shrinking seems to be able to draw that excess outward curve back in. And with all the shrinking work that I've already done, there's still a wave in the panel that's taking more filler than I'd prefer. The nose section I think I could live with.
But then there are other issues. All the under-bonnet front sheet metal ahead of the radiator is damaged to a degree. It was crudely hammered out in the old repairs. Besides looking ugly when you open the bonnet, it's interfering with getting the correct alignment of the body panels that I'm repairing. In addition to the lower fender panel being misshapen, it has also been attacked by the tin worm at its lower extremity. From the outside it looks good, but there were a couple of rust pinholes that I welded up, and a larger deeply pitted area where the chance of ongoing rust-through is a concern.
Replacement wings disappointment
Fitting of the new aftermarket RH side front fender was disappointing. It had several issues that would be considerable work to mitigate.
First, the door gap was huge and uneven, even with the door moved forward as far as possible. The door-edge of the fender is malformed as it doesn't have the nearly 90 degree step bend at the edge of the original, but instead, a very shallow bend which exaggerates the gap. Also, the bead that runs above the side trim strip is too shallow. This could be filled with body filler to simulate the correct geometry, but there was another problem...The inner structure of the fender causes it to stick out too far. It would be necessary in this case to cut and re-weld the inner support member to be able to draw the fender in closer. Another problem was that the alignment along the hood line was bad, with the hood (bonnet) arched up considerably higher.
Rear hatch shut lines
Getting close to finished with the back, I got the hatch panel gap tuned pretty well. Had to run a weld bead along one edge to build it up a little, then approached from the other side by raising the opening with a bit of the DynaGlass filler. The glass reinforced filler is preferable on corner edges like this where standard filler could easily get chipped off.
On the other hand, the DynaGlass doesn't spread smoothly as a finish filler. It's best used for bulk filling where high strength is needed. It will be necessary to do the fine levelling with a finish filler.-
Cleaned away the rust from the rocker with a wire wheel, and it revealed some rust through. So this would be cut out and patched. Inner ...
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Repair work to the right-hand side dogleg was virtually the same as the left-hand side. Inside rocker looked much the same as the other si...
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Before fitting the new replacement panel, the attachment surfaces on the wing need to be cleaned up and prepared for welding. But there ...